MASONRY
Number 1
Substitute
Materials: Replacing Deteriorated Serpentine Stone with Pre-Cast Concrete
Robert M. Powers
Mid-Atlantic Regional Office
National Park Service
SIX
LOGAN CIRCLE
Washington, D.C.
Constructed in 1878 from the designs of architect Henry R. Searle, Six Logan
Circle is a five-story rowhouse which features a highly articulated façade
of green serpentine stone laid up in a veneer of quarry-faced, random ashlar
blocks with Pennsylvania red brick trim. Located in the Logan Circle National
Register Historic District in Washington, D.C., this building sits directly on
Logan Circle, an original open space design element of the 1790s plan for the
Federal City by Pierre L’Enfant.
Constructed for Naval Commander Allen V. Reed, the property remained
a single-family residence until 1940 when the Reed family sold the building.
Typical of many
of the large residential properties within the district, Six Logan Circle was
subdivided and converted into a multiple-unit dwelling after World War II. Over
the next forty years the building functioned as a nine-unit apartment complex
and received little maintenance during this time.
In 1982, the property was purchased by the Six Logan Circle Associates
with the intent of rehabilitating the property into six residential units.
A major component of the rehabilitation focused on selecting a treatment
for the extremely deteriorated serpentine stone façade.
Problem
Serpentine stone was frequently used as a building material in the late
19th century because of its distinctive greenish color. Numerous residential
and moderate-scale institutional buildings were constructed using serpentine
for entire facades or simply as a trim material in urban areas such as
Philadelphia, New York, Washington, Baltimore, and Chicago, as well as
in rural areas close to the quarries such as Chester County, Pennsylvania,
and northern Maryland. However, serpentine’s popularity was short-lived
because of its fragility.
Serpentine is a soft stone composed primarily of hydrous magnesium silicate
which is basically the same mineral found in talc. It is not tightly consolidated,
but a fibrous material that tends to absorb water. The presence of water accelerates
the deterioration of the stone due to the effects of the expansion and contraction
of the stone during freeze/thaw cycles. Since serpentine is an alkaline stone,
it is also sensitive to attacks from sulphuric and sulphurous acids, and carbon
dioxide dissolved in rainwater.
A stone consultant was retained to assess the condition of the serpentine stone
and to recommend remedial work. The consultant conducted an in-depth visual
inspection and evaluation and concluded that the serpentine stone was spalling
extensively, due to the inherent softness and poor quality of the stone and
the chemical forces interacting with the stone. The deterioration had been
further exacerbated by the general lack of maintenance the building had received
for the last forty years which had allowed large amounts of moisture to penetrate
the stone. Moisture, laden with acids, had entered the stone through open mortar
joints and the delaminated surface, accelerating the stone’s deterioration.
In this case, the problem was compounded by additional moisture spilling onto
the surface of the serpentine from clogged, leaky, and inoperable gutters,
downspouts and drains. Given the inherent problems with serpentine stone as
an exterior building material and its overall advanced deterioration on Six
Logan Circle, the consultant recommended that the serpentine stone, which was
used as a veneer covering structure brickwork, be replaced rather than attempting
to repair using traditional patching techniques. This conclusion was supported
by a survey undertaken to determine how many of the stones retained their integrity
(i.e. how many remained substantially free of fractures and crumbling and retained
their surface tooling, texture, and shape). The survey showed that 868 of the
original 946 face stones which made up the façade no longer retained
their integrity. In fact many were so deteriorated that they could literally
be pulled apart by hand.
Solution
Because only 78, or less than nine percent, of the stones remained intact,
total replacement of the historic stone was justified in this particular
case. However, the replacement material needed to closely match the historic
stone in size, shape, dimension, texture and color in order to preserve
the historic character of the façade. To meet these requirements,
three replacement alternatives were considered:
1. Replacement in kind with new serpentine stone
2. Replacement with another type of natural stone
3. Replacement with a substitute material such as pre-cast concrete
Although replacement in kind is generally the preferred preservation
approach when dealing with a non-repairable material, serpentine stone
is no longer quarried for use as an exterior building material due to
its poor performance historically. It is thus not readily available for
large-scale applications such as that proposed for Six Logan Circle.
An alternative stone (such as limestone) could be cut to match some of
the visual characteristics of serpentine, but it could not duplicate
its distinctive green coloring. Therefore, the material that offered
the most potential for use as a replacement material was pre-case concrete.
This material had recently been used to replace extensively deteriorated
brownstone on the Renwick Gallery of the Smithsonian Institution in Washington,
D.C., and it was determined by the consultant (who had worked on the
Renwick Gallery restoration), that the same technology could be successfully
applied to replace the serpentine stone at Six Logan Circle.
Work Description
Before the new cast stone could be manufactured, the existing serpentine
stone façade had to be recorded. An architecture student was hired
to measure each existing stone on the façade and prepare precise
drawings of the elevation, showing the size and location of each stone.
Each stone was assigned two numbers—an individual identification
number and a number indicating the stone’s shape and size. These
key numbers were marked directly on the measured drawings. Drawings were
prepared for the plainer stones that made up the major portion of the
façade as well as the decorative trim stones. From
these drawings, a master list of all the stones and their sizes was compiled,
which was used to guide the casting and manufacturing processes. Later,
as each new stone was fabricated, it was noted on the drawing so that
an up-to-date inventory could be maintained. As revealed by the earlier
condition assessment survey, 78 intact stones still displayed their original
shapes, sizes and textures. These particular stones were fortunately
diverse enough to provide a representative sampling of the entire façade
and thus served as models for reproduction. The following process was
used to reproduce the shape, size and surface texture of the serpentine
blocks:
1. A release agent was sprayed on each stone of the façade to
be reproduced.
2. Latex molding rubber was then brushed-on in layers to the surface
of the stone, still in-situ, to obtain an impression of the stone’s
surface. From these latex molds, the surface qualities of the individual
blocks of the serpentine façade could be faithfully reproduced
in the casting process.
3. The latex mold was removed from the stone and in the workshop the
mold was built up with plaster to increase the crispness of the details.
4. This built-up mold, when placed in a specially constructed wooden
framework reinforced with steel rods and bolts, became the casting for
the mold.
5. A release agent was applied over the formwork and the built-up mold.
Then the concrete was poured into the casting mold.
Although the above process worked well for over 90% of the stones to
be replicated, the remainder of the stones needed for models were too
deteriorated to take a face impression in-situ. In those situations,
the stone was carefully removed from the wall and these additional steps
were followed:
1. A bonding agent was applied to the surface of the stone to be reproduced.
2. Using the more intact stones as models, the stone’s surface
was built up with a mixture of portland cement and sand to approximate
as closely as possible the stone’s original surface, shape, and
texture.
3. After the built-up stone was dry, the same process described earlier
was followed to create molds of these stones.
The owners were fortunate enough to have a rear yard large enough to
establish an approximately 1,100 square feet workshop on-site for manufacturing
the new pre-case concrete units. By casting the stones on-site instead
of sending the molds to be poured at another location, they eliminated
shipping costs. The enclosed temporary shed constructed to house the “manufacturing
plant” consisted primarily of a stud wall system which polyethylene
wall covering. Portable kerosene heaters provided heat for the workmen
as well as the warm temperatures necessary for the stone manufacturing
and curing processes during the winter months.
The process of manufacturing the new concrete stones was carried out by a crew
consisting on the average of three laborers to make molds and take impressions,
and four laborers responsible for removing the cast units from the molds and
cleaning them. These workers were under the supervision of the consultant and
the contractor who trained them in each step of the process. The process consisted
of five steps:
1. Measuring and mixing the materials
2. Checking for quality control
3. Pouring and vibrating the concrete
4. Air curing, mold removal and inspection
5. Removing soluble salts by submerging in a water tank.
Mixing the Materials
The concrete mix was composed of the following materials:
·
White portland cement meeting ASTM C-150 Type I Standards
·
Inorganic masonry pigment, chromium oxide green as manufactured by Mineral
Pigments Corporation
·
Coarse aggregate (gravel) 3.8 to #4 “Eau Claire”, dry and
bagged
·
Fine aggregate (concrete sand), “Eau Claire” passing a #16
screen, dry and bagged
·
Air-entraining agent (liquid admixture of the vinsol resin type conforming
to ASTM 260-77)
·
Water-reducing agent, liquid type conforming to ASTM C-494, “Chemical
Admixture for Concrete,” Type A (Pozzolith 122-N)
·
Water, clean, clear, potable with a pH reading between 5-8 and the conductivity
not exceeding 100 MILLIMHOS on the 0-200 scale.
These materials were mixed in a paddle mixer large enough to combine
the materials so that each batch would not exceed the number of molds
that could be vibrated without tempering the mix with water. Each day,
before the start of mixing, a minimum of 2 cubic feet of design mix “butter” was
run through the cleaned mixer and dumped. This procedure seasoned the
mixer. If another batch was mixed within 30 minutes, the remnants of
the previous batch was used as the “butter”. The mixer was
cleaned at the end of each day.
Finding the exact concrete mix to replicate the color and appearance
of historic stone is usually a matter of some experimentation. However,
in this case, by using the successful formula derived in part from the
work on the Renwick Gallery, the only major obstacle was finding the
proper pigment color that would match the serpentine stone, and would
not fade. After a series of test stones were manufactured and fully cured,
a close color match was established. The mix that produced a color closest
to that of the serpentine stone, and also meeting all the required strength
tests, was composed of the following materials in the quantities indicated
(the quantities shown are in pounds for ½ cubic yards):
·
White portland cement- 376 lbs.
·
Pigment- 12 lbs.
·
Fine aggregate- 700 lbs.
·
Coarse aggregate- 775 lbs.
·
Water- 150 lbs.
·
Vinsol resin- 4 oz.
·
Pozzolith 122N- 18 oz.
These materials were combined in the following sequence:
·
Fine and coarse aggregate
·
Maximum of 2/3rds of the water
·
White portland cement
·
Pigment
·
Admixtures
·
Remaining water
The materials were combined in the mixer until there was a consolidated,
homogeneous concrete of the required slump—usually about two to
three minutes and always less than ten minutes.
Quality Control
Once the materials were thoroughly mixed and ready to be poured, measures
were taken to ensure that the newly-fabricated pre-cast units met the
specified strength criteria. In the manufacturing process adopted for
Six Logan Circle, a minimum of 6 standard testing cylinders (6”x12”)
were filled from a selected batch once a day, and sent to a testing laboratory.
Two of the cylinders were tested for compressive strength at 7 days and
at 28 days. The remaining cylinders were retained for 56 days for additional
testing before disposal. A minimum of 2 standard 6”x12” cylinders
cast from all the other batches was collected and also tested for compliance
with the design criteria of 5,000 psi at 28 days.
Pouring the Concrete
The consolidated and homogeneous concrete mix was poured from the mixer
into the specified mold which had already been placed on the vibration
table. The vibrating process forces the entrained air and surface air
out of the mold, eliminating in most cases the possibility of surface
imperfections from air bubbles. Proper vibration of the newly poured
concrete was extremely important to obtain a high quality pre-cast concrete.
The vibration table operated at a rate of 2,600 vibrations per minute
and could accommodate all the castings from a batch within thirty minutes
after mixing. Small cast units required approximately sixty seconds of
vibration and the larger ones required approximately ninety seconds.
A cake spatula was effective in cutting many of the air bubbles from
the surface of the sides of the mold during the first ten seconds of
the vibration process.
Air Curing, Mold Removal and Inspection
After the vibration process was completed for each stone, the molds
were placed on heated benches for sixteen hours, after which the molds
could be gently removed without damaging the stone. Each stone was then
inspected for any visual inconsistencies or other imperfections from
the mixing, pouring and vibrating process. The stones were evaluated
for problems such as uneven or non-matching coloring, chips, exposed
aggregate, air bubbles (pin holes), or depressions. During the manufacture
of the new pre-cast stone, more than 400 newly cast stones were rejected
due to surface deficiencies.
Removing Soluble Salts
The final step in the manufacturing process was essential to the successful
outcome of the product. In this step, the stones were submerged in a
water tank for a period of six hours, then removed and dried for six
hours. The drying process forced soluble salts inherent
in the concrete mix to the surface of the stone. An application of a
weak solution of muriatic acid with a thorough water rinse was used to
wash away the leaching salts. The procedure of soaking and drying was
repeated three times for every stone. After completing this process,
each stone was transferred to the basement for storage on wooden skids.
Installation
Before any of the original stone was removed, the corresponding section
of pre-cast material was arranged in the “staging area” in
the basement. Using the measured drawings and numbering system prepared
earlier, the blocks of cast stone were assembled on the basement floor
on top of 4” of sand. Assembling them in the staging area allowed
for final inspection for the blocks and also allowed the master mason
to arrange the new stones during a “dry run” prior to the
actual installation on the building, thereby minimizing problems once
the work on the building began.
Once all the new pre-cast concrete blocks were manufactured, inspected and
fully cured, the process of dismantling the existing deteriorated façade
and installing the new material began. Since the serpentine stone was used
as a veneer covering structural brickwork and was not itself a structural element,
sections of the veneer could be removed without jeopardizing the stability
of the building.
With the front elevation fully scaffolded, sections of the serpentine stone
and ornamental brick were removed. Because the brick trim was in excellent
overall condition and was to be reused in the new façade, it was carefully
removed with hand tools, inventoried, and stored for reinstallation. With the
serpentine and face brick removed, necessary repairs were made to the structural
brick, and stainless steel anchors for the new pre-cast veneer were installed.
The new cast stones were hoisted up the scaffolding on wide belt slings with
an electric winch and installed in place.
Since the new pre-cast concrete blocks are much harder than the original serpentine
stone, a mortar mix containing a large proportion of white portland cement
was used. However, other than the composition, the new mortar joints match
the light-colored, raised mortar joints used on the original stone façade.
The walls were then backfilled with a parching material.
The original bricks were individually cleaned with bristle brushes and water
before being reset into the new façade. The new brick mortar was based
on an analysis of the original, dark colored brick mortar and matched it in
composition, color, texture, joint width and profile.
Project Evaluation
After nine months of work, the installation of the new pre-cast façade
for Six Logan Circle was completed at the cost of $225,000, or slightly
less than one-forth of the total project cost. The project was considered
a success by all the participants; the stated goal of removing the crumbling
serpentine veneer and replacing it with a new material that returned
the façade to its original appearance was met. The building has
a renewed presence with its pre-cast concrete units molded to match the
form of the original detail, texture and color that had been absent for
many years.
Some of the trim pieces, in particular the floral blocks as well as units in
the belt coursing and window sills, do have noticeable surface imperfections
when viewed up close, such as indentations caused by air bubbles and in a few
instances the aggregate is exposed, indicating a poor concrete mix. Ideally,
each of these units should have been rejected during the inspection state.
However, the small number of such pieces does not detract from the overall
appearance of the rebuilt façade.
The manufacture and installation of the new pre-cast concrete units and historic
brick was an expensive undertaking; however, in this case, alternative options
were very limited. The new owners chose this course of action because of their
desire to find a long lasting solution to a difficult problem. This approach
may not be appropriate in all situations involving deteriorated serpentine
or other types of historic masonry. Total replacement of the deteriorated stone
veneer of a historic building using a substitute material should be considered
only after careful analysis. If, after a thorough examination of all possible
alternative treatments, a replacement approach is selected, the project should
be undertaken only by qualified personnel under professional guidance and supervision.
PROJECT DATA:
Building:
6 Logan Circle
Washington, D.C.
Owner:
Six Logan Circle Associates
James F. Smith and Allan G. Bortel, General Partners
Washington, D.C.
Project Dates:
November 1984- July 1985
Stone Consultants:
Gary R. Brenner
Gaithersburg, Maryland
Dr. Seymour Lewin
New York University
New York, New York
General Contractor:
Construction Consultant Services, Inc.
James F. Smith, President
Washington, D.C.
Project Cost:
$1,044,804- Total project rehabilitation cost
$233,000- Replacement of masonry veneer using new pre-cast units and
original bricks—includes material, equipment and labor
This PRESERVATION TECH NOTE was prepared by the National Park Service.
Charles E. Fisher, Heritage Preservation Services, National Park Service,
serves as the Technical Editor for the PRESERVATION TECH NOTES. Information
on the cast-stone replacement system described here was supplied by James
F. Smith, General Partner and Contractor for the project, and Gary R.
Brenner and Seymour Lewin, project consultants. Special thanks to the
following National Park Service staff who contributed to the production
of this Tech Note: Martha Raymond, Dennis Montagna and Varnetta Ross
of the Mid-Atlantic Regional Office, and Anne Grimmer, Theresa Robinson
and Brenda Siler of the Preservation Assistance Division.
PRESERVATION TECH NOTES are designed to provide practical information
on innovative techniques and practices for successfully maintaining and
preserving cultural resources. All techniques and practices described
herein conform to established National Park Service policies, procedures,
and standards. This Tech Note was prepared pursuant to the National Historic
Preservation Act which direct the Secretary of the Interior to develop
and make available to government agencies and individuals information
concerning professional methods and techniques for the preservation of
historic properties.
Comments on the usefulness of this information are welcomed and should
be addressed to PRESERVATION TECH NOTES, Technical Preservation Services,
National Center for Cultural Resources, National Park Service, 1849 C
Street, NW, (2255) Washington, DC 20240.
This publication is not copyrighted and can be reproduced without penalty.
Normal procedures for credit to the author and the National Park Service
are appreciated.
|